hb1
New Member
Hi, I just purchased a Simrad TP32. While testing it, I noticed, that both in standby and auto mode, as soon as the push rod reaches the end position, the TP32 trips out for a few seconds.
When in standby mode, I use the buttons to control the push rod. When the end position is reached, the device trips out and I have to wait for 3-4 seconds until I can control the rod again.
In auto mode, when the end position is reached, the device trips out and after 3-4 seconds it goes back to standby. It does this at both end positions. Did someone else experience this? Am I doing something wrong?
Also, I noticed, the manual is saying that the typical current consumption in auto mode is around 500mA. Is this an average value? I'm asking this, as when moving the push rod, the current is between 1-2A. Many thanks
When in standby mode, I use the buttons to control the push rod. When the end position is reached, the device trips out and I have to wait for 3-4 seconds until I can control the rod again.
In auto mode, when the end position is reached, the device trips out and after 3-4 seconds it goes back to standby. It does this at both end positions. Did someone else experience this? Am I doing something wrong?
Also, I noticed, the manual is saying that the typical current consumption in auto mode is around 500mA. Is this an average value? I'm asking this, as when moving the push rod, the current is between 1-2A. Many thanks
