rotrax
Well-Known Member
Returning from the mooring last Monday I noticed no water stream from the telltale.
The engine was commisioned in July 2007 and untill 2015 had had less than 2 hours running-the previous owner kept a log. I checked and serviced it in 2016, again in 2017 and again at the start of this season. It had always been faultless.
Anyway, fetched it home, pulled the gearcase off and inspected the impeller-looked perfect. Cleaned it all up, put the impeller back in-checking it was properly located on its drive key-refitted the gearcase and started the engine, good output from the telltale. Stopped the engine, greased and lubed a couple of pivots and the tilt lock, restarted the engine.
No output from the telltale! I am running it in a full dustbin of water, so the intake is well submerged.
Before I start chasing shadows, any direct experience on here with similar problems?
The re-used impeller required a prod on the tips to fit back into the pump housing and I did expect it to be springy enough to work-next step will be to change it I expect.
I fitted a rubber pipe on the water pipe that transfers water up to the engine and blew through-no resistance and could hear the displaced air in the exhaust. The pee hole is also clear. As a matter of course the engine is run in fresh water every time we return to the outboard store at our club mooring, so I dont think salt build up is an issue. I doubt it has run 12 hours since it was new. Longest single run was Dittisham-Totnes and back this year, 2 hours total, and completly trouble free.
Any help gratefuly recieved.
The engine was commisioned in July 2007 and untill 2015 had had less than 2 hours running-the previous owner kept a log. I checked and serviced it in 2016, again in 2017 and again at the start of this season. It had always been faultless.
Anyway, fetched it home, pulled the gearcase off and inspected the impeller-looked perfect. Cleaned it all up, put the impeller back in-checking it was properly located on its drive key-refitted the gearcase and started the engine, good output from the telltale. Stopped the engine, greased and lubed a couple of pivots and the tilt lock, restarted the engine.
No output from the telltale! I am running it in a full dustbin of water, so the intake is well submerged.
Before I start chasing shadows, any direct experience on here with similar problems?
The re-used impeller required a prod on the tips to fit back into the pump housing and I did expect it to be springy enough to work-next step will be to change it I expect.
I fitted a rubber pipe on the water pipe that transfers water up to the engine and blew through-no resistance and could hear the displaced air in the exhaust. The pee hole is also clear. As a matter of course the engine is run in fresh water every time we return to the outboard store at our club mooring, so I dont think salt build up is an issue. I doubt it has run 12 hours since it was new. Longest single run was Dittisham-Totnes and back this year, 2 hours total, and completly trouble free.
Any help gratefuly recieved.