jrudge
Well-Known Member
So how is everyone doing so far?
Compared to Williams Rib hell last year and Generator misery the year before ( which only lasted 3 days to be fair) my tally so far has been reassuringly mild.
Boat is a Squadron 58 2004.
1. Flat rib battery. Assumed needed replacement but surprisingly not
2. Generator stopped. No Coolant flow. Turned out to be a tiny chafe hole in the supply pipe ( that had anti chafe binding on it ex factory so it laster 14 years) which was suddenly not so tiny. Bunged it up with leak stop for lunch and E30 an an hour later all fixed. Had not been self priming for a while so I suspect that is why.
3. Ice Maker. Flow hose had perished. Due to spectacular design all water is over the electrics ( anyone thought of doing it the other way round) so any leak pops the power. There was spare hose so cut and re connected. Same the following day. Hose dead so replaced. Ice making restored. Few days later same again. This time ice maker off, as it defrosts bit of water flows out the front and over the switch ( which is again below the water ...). Fixed with a dab of silicone
4. No water from the taps. Have 2 water pumps. Turns out one does not work ( new one ordered- boats.co.uk say the bottom one always fails). The second one had a combination of the wires falling off the pressure sensor ( which whilst a simple job are almost impossible to get back on as they face away from you at arms length) and then a faulty pressure switch which was solved with a clout from a pair of pliers. Will remove the lot, replace pump and set up property by adjusting pressures on next visit.
5. An unfeasible number of the cr%& LED bulbs I bought have failed. Halogen would have been more reliable. New batch bought.
6. The radar ( which I never use but turn on from time to time to pass the day away!) has stopped revolving. I will investigate next time I am there. Drive belt / fuse / connectors I suspect. We will see. It does not really bother me.
As usual nothing stopped it moving, no dismantling of toilets and the AC worked fine - so all in I would call it a success!
Compared to Williams Rib hell last year and Generator misery the year before ( which only lasted 3 days to be fair) my tally so far has been reassuringly mild.
Boat is a Squadron 58 2004.
1. Flat rib battery. Assumed needed replacement but surprisingly not
2. Generator stopped. No Coolant flow. Turned out to be a tiny chafe hole in the supply pipe ( that had anti chafe binding on it ex factory so it laster 14 years) which was suddenly not so tiny. Bunged it up with leak stop for lunch and E30 an an hour later all fixed. Had not been self priming for a while so I suspect that is why.
3. Ice Maker. Flow hose had perished. Due to spectacular design all water is over the electrics ( anyone thought of doing it the other way round) so any leak pops the power. There was spare hose so cut and re connected. Same the following day. Hose dead so replaced. Ice making restored. Few days later same again. This time ice maker off, as it defrosts bit of water flows out the front and over the switch ( which is again below the water ...). Fixed with a dab of silicone
4. No water from the taps. Have 2 water pumps. Turns out one does not work ( new one ordered- boats.co.uk say the bottom one always fails). The second one had a combination of the wires falling off the pressure sensor ( which whilst a simple job are almost impossible to get back on as they face away from you at arms length) and then a faulty pressure switch which was solved with a clout from a pair of pliers. Will remove the lot, replace pump and set up property by adjusting pressures on next visit.
5. An unfeasible number of the cr%& LED bulbs I bought have failed. Halogen would have been more reliable. New batch bought.
6. The radar ( which I never use but turn on from time to time to pass the day away!) has stopped revolving. I will investigate next time I am there. Drive belt / fuse / connectors I suspect. We will see. It does not really bother me.
As usual nothing stopped it moving, no dismantling of toilets and the AC worked fine - so all in I would call it a success!