neilf39
Well-Known Member
Make an access hole in the bulkhead and fit a plastic access hatch of 4 or 6 Inches in diameter. Will look quite neat and costs a fiver on ebay.
& take half a day to fit, for a job that should take less than 5 minutes .Then one still has to get 2 hands through the hole to hold nut & unscrew the screwMake an access hole in the bulkhead and fit a plastic access hatch of 4 or 6 Inches in diameter. Will look quite neat and costs a fiver on ebay.
Unfortunately, should is the operative word I suspect the OP's already spent a lot more than 5 minutes on it already, not to mention that the swear box must be filling up nicely.for a job that should take less than 5 minutes
One canGo rusty in 5 minutes, unless one can get SS ones
Cut the hole for the hatch, then do the job before fitting the hatch surround - as then slightly more space and hopefully smoother edge& take half a day to fit, for a job that should take less than 5 minutes .Then one still has to get 2 hands through the hole to hold nut & unscrew the screw
That is exactly how my access panels were madeThanks for all the advice. Some ideas I had not thought of.
Decision made, I am going to cut an access hole from the qurter berth. The reason I have decided this route is the plywood panel supporting the water tank will not be damaged in any way and when refitting the tank I can securely bolt the corner down. When full the 60 gallon water tank weighs 600lb, so keeping that securely fixed is important. Also if I ever need to remove the diesel tank, I can also access the corner bolt in the same position. The opening can be made any size I decide, rather than a fixed hatch size. The cover will be made using the cut out and an overlapping piece of 5.5mm plywood secured to it for the fixing screws to hold it in place. This will be covered with foam backed vinyl, which I have plenty, to match the rest of the quarter berth lining and the screws will be covered with vinyl covered caps. This will make it look like a professional job.
When it is finished I will post some photos.
Just as a further comment, I already have a hatch at the foot of the quarter berth to access the port aft quarter. It really is not quite big enough, so I may in the future decide to make it larger.


The tank is sound. All that has happened is the weld on the outlet has rusted. The rest of the stainless tank is looking very good. When it is repaired, it will be pressure tested to ensure there are no other leaks.Well done: you've made a neat job of that.
Given (a) that the tank has started to deteriorate and leak and (b) it is now out of the boat, have you considered simply replacing it? A lighter, plastic tank of a slightly different size and/or shape might make any future work significantly easier. Just a thought.
I used a screwdriver and a spanner. It was still difficult with the access, would have been easier if I was left handed. Also working whilst lying down made it a bit difficult with limited space for my hands. The thread had a build up on dirt, so needed to be undone using the spanner and screwdriver over almost all of the thread. The bolt took about 8 minutes to undo even though it was only about 8 turns. Oh, I do love working on boats.One Q
I assume you used a screwdriver to remove the screw, did it turn easily or was it hard work?
A fellow Fulmar owner had a similar problem and his was just a weld. Probably find out in the next day or two. If it had been a mild steel tank, then yes it would have been changed.If it was an easy part to access, I’d be happy to have it repaired, but given that it’s such a pig to get out, I must admit I’d be thinking about putting in a plastic replacement. Is there an access panel on tank? Are you certain there’s no rust on the inside of that outlet?
What do you call those?
I had much the same on the stainless water tank in my Bav 37 - made in Greece to replace the failed plastic original. Weld corroded around the inlet - hidden of course right in the bows. Only found out when we filled it ready for the trip back across the Med. Promptly dumped most of the 150l into the bilge during the rough first day out of Corfu. Fortunately there was another 150l in the aft tank. Took it out when I got back to UK - massive job as the nice Greeks had wedged it in with wood blocks and then foamed it. Took me a week on and off to get it out. Had it welded up with a plate around the leaking inlet and did the same around the outlet. Had brackets welded on so that I could bolt it in. Glassed in a new platform and mini bulkhead for the brackets. Proper job. Very secure and easy to remove should there be further problems.A fellow Fulmar owner had a similar problem and his was just a weld. Probably find out in the next day or two. If it had been a mild steel tank, then yes it would have been changed.
What do you call those?