groob32
New Member
I have installed a new EV1, ACU100, P70 and wheeldrive as a replacement for an old ST4000 with a old black Mk 1 wheeldrive on my Jeanneau 32.2, and as an autopilot is is a big improvement. Unfortunately the compass (on top a standard binnacle) now has up to 18 degrees deviation (down from 30 or so before I repositoned the motor at the bottom of the wheel, slightly further from the compass). If I remove the wheel with drive and motor attached the deviation goes, so it seems it can only be the motor.
Raymarine have confimed that the new motor is more powerful but have not come up with anything more helpful. Is this something anyone else has encountered?
Raymarine have confimed that the new motor is more powerful but have not come up with anything more helpful. Is this something anyone else has encountered?